contact_printer/ino
Matt McWilliams 1aca2dd5c0 Motor behavior is stable. Discarded one of the L298N boards: now we can run the drive motor off one channel and both takeup motors off another. DO NOT USE LESS THAN 2A. Using 1.3A the motor controller board draws too much and shuts it down. Removed the rerences to Picture/Stock and am just using takeup. All progress at Worm. 2024-02-20 22:11:13 +01:00
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contact_printer Motor behavior is stable. Discarded one of the L298N boards: now we can run the drive motor off one channel and both takeup motors off another. DO NOT USE LESS THAN 2A. Using 1.3A the motor controller board draws too much and shuts it down. Removed the rerences to Picture/Stock and am just using takeup. All progress at Worm. 2024-02-20 22:11:13 +01:00
contact_printer_old Rough draft of new contact printer library and class layout. 2023-05-25 08:32:42 -04:00
esp32_dc_motor_poc Test second set of pins 2024-02-20 12:17:39 +01:00
jog_motor Add placeholder jog_motor sketch in case motors need to be adjusted during use. 2024-02-18 10:34:19 -05:00
motor_encoder_poc Bevel the sprockets and add reinforcement to let a bearing fit without issue. 2024-01-25 19:47:32 -05:00