Prevent motor from stopping before 100ms. Took out the logging in watchMicro, due to the fact that the problem with backwards frames was likely a bad connection.

This commit is contained in:
mmcwilliams 2018-01-08 22:08:41 -05:00
parent b114ef8b0e
commit a9414c6212
1 changed files with 2 additions and 4 deletions

View File

@ -236,11 +236,10 @@ intval._watchMicro = function (err, val) {
if (err) {
log.error('_watchMicro', err)
}
log.info(`Microswitch val: ${val}`)
//log.info(`Microswitch val: ${val}`)
//determine when to stop
if (val === 0 && intval._state.frame.active) {
//&& (now - intval._state.frame.start) > 100
if (!intval._state.micro.primed) {
if (!intval._state.micro.primed && (now - intval._state.frame.start) > 100) {
intval._state.micro.primed = true
intval._state.micro.time = now
log.info('Microswitch primed to stop motor')
@ -375,7 +374,6 @@ intval.frame = function (dir = null, exposure = null, cb = () => {}) {
log.info('frame', {dir : dir ? 'forward' : 'backward', exposure : exposure})
intval._pause()
if (dir) {
intval._startFwd()
} else {